Frankspolara
New Member
Hello everyone -
My car is a 1968 Polara 383 originally 2 bbl. I had a 4bbl intake from a 67 383 laying around and decided to upgrade (replace) using that manifold and an Edelbrock 1406 (plan was to eventually replace the cam, timing chain, lifters).
Here is the issue that developed:
First drive of the day, the car will intermittently and randomly skip - not like a misfire, but enough to rock you during mild/light acceleration. Every once in a while - very infrequent, you'd hear a pop/backfire from carb. The one or two times I was able to look at the tach and steer this car straight, you could see it drop momentarily. can't really hear it at idle but did at one time when it was cold and on fast idle.
After the first drive, if the car sits, it runs great until the next morning. Because of this, it makes troubleshooting difficult and we're quickly running out of summer.
Here is what I have done:
Thanks for your help/advice!
My car is a 1968 Polara 383 originally 2 bbl. I had a 4bbl intake from a 67 383 laying around and decided to upgrade (replace) using that manifold and an Edelbrock 1406 (plan was to eventually replace the cam, timing chain, lifters).
Here is the issue that developed:
First drive of the day, the car will intermittently and randomly skip - not like a misfire, but enough to rock you during mild/light acceleration. Every once in a while - very infrequent, you'd hear a pop/backfire from carb. The one or two times I was able to look at the tach and steer this car straight, you could see it drop momentarily. can't really hear it at idle but did at one time when it was cold and on fast idle.
After the first drive, if the car sits, it runs great until the next morning. Because of this, it makes troubleshooting difficult and we're quickly running out of summer.
Here is what I have done:
- Prior to upgrade I installed the Pertronix Electronic Ign, cap, wires and plugs. Car ran fine.
- After replacing the carb and manifold is when the problem started.
- Replaced the coil, rerouted and checked ign wires esp 5&7 - all tightly plugged in.
- Replaced the cap again
- Installed a new manifold and gasket (Edelbrock 2186)
- Checked rechecked and varied timing
- Ran without vacuum advance connected and plugged
- Fuel filter
- New kick-down
Thanks for your help/advice!